A Maintenance Oriented Podcast For Airplane Owners, Pilots, and Mechanics

Tag: exhaustvalve (Page 2 of 2)

137 – IA Seminar Borescoping and Exhaust Valve Stories

Yesterday, I had an opportunity to present a talk at our local IA renewal seminar about exhaust valve borescoping.

I shared some of my favorite pictures – the ones that demonstrate how critically important borescoping is, and that compression testing alone is not sufficient.

The following three examples are especially startling, since they showed a compression test of at least 60/80, but were in imminent danger of in-flight failure:

The FIRST ONEis from a Continental engine in an A36 Bonanza. Notice the green area at 9:00, indicating that area was in danger of a piece breaking off the edge.

The SECOND ONEis from another Continental engine, also an A36 Bonanza. The compression of this one was 61/80, but there was a chunk missing from the edge, with a crack toward the center of the valve!

The broken edge still had enough area to seal for a compression test:

And the THIRD ONE was from a Lycoming engine in a Cessna 152. Take a look:

In the previous three examples, the borescope was absolutely necessary to discover these dangerous and unairworthy exhaust valves.

For comparison purposes, the following two pictures are examples of healthy exhaust valves:

I also shared some pictures of valves that other people have removed from their engines.

The following is from Sylvan Martin’s Grumman Tiger with a Lycoming O-360 engine. Sylvan was able to land safely after his engine ran slightly rough. He said, “My opinion is that cylinder 1 would have been noticeable at a minimum of 150 hrs before it deteriorated to the point of cracking that far across the face… Compression check will help w/ ring problems, but our family’s experience in industrial diesels (power generation) is that rings fail slowly/predictably while valves fail suddenly/catastrophically…..”

He later had to change two other cylinders, after the borescope indicated they were burning:

(Previous three photos courtesy of Sylvan Martin.)

Jason Figueroa had to change a cylinder on his Cherokee 235’s Lycoming O-540 engine due to a burning exhaust valve that was found with a borescope.

(Photo courtesy of Jason Figueroa.)

Jason said, “Borescoping told us we had an impending problem, and led to catching it before it failed.”

Here are two more exhast valve pictures from an unidentified source:

I’m convinced this broken valve could have been detected with a borescope LONG BEFORE the edge broke off.

My hope is that all of us who have the responsibility of determining the airworthiness of piston engines in airplanes, will use a borescope along with the compression tester for higher levels of safety and reliability.


Do you have a dream to fly? If so, you might be encouraged by the poem I shared at the end of my talk yesterday. My daughter sent it to me one day last Summer… it’s called, “The Dream Does Not Die!” If you’re interested, be sure to listen to the last part of the audio.

131 – Drew Wright’s Cessna 182 Exhaust Valve Lapping Success!

During the recent annual inspection on Drew Wright’s Cessna 182, cylinder #1 had a low compression of 42/80. However, with the amazing technology of borescoping, he was able to take a look inside the cylinder. The nice concentric circle of deposits on the face of the exhaust valve indicates a healthy valve. Drew wondered if perhaps this valve would be a good candidate for lapping in place, without removing the cylinder.

Even though the valve appeared healthy, Drew noticed a significant amount of air leaking out the exhaust during the compression test. Once again, his borescope was very helpful in observing the condition of the exhaust valve and seat area. The valve looks good, except for the rough and uneven seating area.

The seat also looks good, except for the corresponding rough and uneven seating area.

With the supervision of his A&P, Drew was able to remove the rocker cover and the exhaust valve springs. After verifying the valve guide was in good condition with no excessive wear, and the valve was sliding freely in the valve guide, he was ready to “lap” the valve (to apply a small amount of valve grinding compound to the edge of the valve using a long Q-tip through the top spark plug hole, and spinning the valve against the seat to smooth out and improve the seating area.)

Drew used a piece of wood dowel rod, some clear tubing, and some hose clamps, for this task… I like his idea so much, I’m planning to use this technique in the future.

One of the most important parts of the lapping process, is cleaning out the residue after the job is finished. One method is to spray Av-gas into the top spark plug hole to wash the grinding compound off the valve and the surrounding areas, and let it run out the bottom spark plug hole. Multiple washings, along with some compressed air, cleans up the area very well.

An additional thing Drew did was to push a thin cloth into the top spark plug hole, and pull the valve back to squeeze the cloth between the valve and valve seat. Then, he could turn the valve against the cloth and clean the seating area even better. I’m also going to keep that little tip in mind for my next lapping project. Thanks Drew!


The seating area of the valve showed a nice smooth band after the lapping was done – very impressive!

After the lapping was completed, a new rotator was installed on the exhaust valve, everything was reassembled, and the compression immediately improved!

But the best result was the compression test that was done after running the engine… that same cylinder that was 42/80, now had a compression of 78/80! What a fantastic result, and now, hopefully that cylinder will run reliably for many more hours.

Be sure to listen to the audio for this episode for more details about Drew’s adventure. He also shared about an induction leak that was visible because of some blue fuel staining.

After removing the intake pipe, it was obvious the gasket had shifted out of position during the assembly process many years ago… perhaps this was part of the poor idling problem that was also corrected during the annual inspection. After installing a new intake gasket and adjusting the idle mixture setting, the engine idled much better than before.

Drew’s story is a true inspiration in so many ways.

So, if you, as an airplane owner, have an interest in learning and getting involved in the maintenance, just find an A&P who is willing to give you some supervision to keep things legal, and you’ll have all kinds of possibilities.

Well done Drew, on your exhaust valve lapping project! I’m thrilled with the result you achieved on this one!

Drew has a young family, and it makes me happy to know he’s taking such good care of his airplane… after all, he’s got some precious cargo to haul around!

125 – Engine Failure – What Would You Do In A Moment’s Notice?

Not long ago, there was an unusual engine failure in a Cessna 182 at Shenandoah Valley Regional Airport.

Cindy Ferek was the flight instructor on board that day, and she landed the airplane safely on the runway. Before we get into that story, I’d like to introduce Cindy. (The Cessna 172 in the following picture is not the airplane that had the engine failure.)

Cindy taught high school physical education for 21 years at Turner Ashby High School, which gave her an excellent teaching foundation that she uses today as she skillfully works with students in the cockpit of airplanes. Not only is Cindy an excellent flight instructor, but she’s also just an inspiring person to be around! I hope you’ll listen to the podcast to hear about more of Cindy’s story, both in and out of the airplane.

The engine failure we talked about in today’s episode, happened in the traffic pattern, thankfully. Here’s the airplane after they landed safely and parked it in the grass to save the engine:

Shortly after their successful landing, one of the line guys tugged the airplane up to the maintenance shop.


At first it was challenging to figure out what actually happened to the engine, because there was no external evidence of any problems. But a borescope inspection revealed the exhaust valve in cylinder #1 was not opening at all. And after removing the rocker cover, it became really obvious. The rocker arm shaft boss had broken apart and the rocker arm could not operate the exhaust valve.

Thank you Cindy, for sharing a bit of your aviation journey and your engine failure story with us, and for all the excellent work you do to make aviation such an inspiring endeavor to pursue!

For those of you who would like to contact Cindy, there are multiple ways to get in touch with her. (And she would love to hear from you.)

Blog: CindyFerek.Weebly.com

Email: pilotcferek@gmail.com

Cell: 540-607-0251


P.S. One last reminder:

If you work on your airplane, and need to learn to perform excellent safety wiring, check out the “Safety Wire Like A Pro” video tutorial course… It will show you in great detail how to do an excellent job, whether it’s safety wiring an oil filter, a fuel strainer, a brake caliper, or any other item an airplane owner is approved to perform.

Click the following link and check it out:

https://airplane-owner-maintenance.teachable.com/p/safetywiring

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